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1962. In 1962 one of our number got
himself mixed up with a bar-girl who was old enough to be his mother and
had put in a request to marry her. This was refused and it started a run
of incidents that took some time to work out that they were deliberately
introduced rather than being normal faults or servicing errors. They culminated
in a pretty miserable days air firing when I had decided, half way through
the day, that this person couldn't be trusted after he had failed to reset
the relays on the T.7 after the rearm and the aircraft got airborne with
a full load and couldn't fire anything. After this he was put on the end
of the runway for the plugging/unplugging and I thought, incorrectly,
that he couldn't screw up anything out there. The first aircraft took
off and a few minutes later it returns, can't get the wheels up. The aircraft
lands and we de-arm and send it to the hangar where they do retraction
tests, no problem. The aircraft comes back on line and we re-arm and off
it goes again, same problem only this time I am watching the end of runway
operator with the binoculars. I jumped in the Land Rover and went out
to the unplugging point, when the aircraft lands I go to the port wheel
well myself and find that the 5-pin plug had never been plugged in. Problem
solved. The offending person was removed from the line and transported
to the SengO's office where the situation was explained. The rest of the
air firing went off without incident. The overall result was no more air
firing or maintenance incidents and the person concerned was quickly posted
to Gan to complete his tour.
I got a couple of trips in the T.7 (WV383) and on one of them we (pilot
Fl/Lt Crichton) broke the sound barrier in a dive out over the sea. The
Hunters gave us few problems although they didn't seem to be as well suited
to the low-level round-the-mountains role as the Venoms, which seemed
to be more agile. We had a wheels-up landing (Fl/Lt Crichton) due to only
the nose and stbd main wheels coming down. The pilot elected not to use
the emergency system, as he would be stuck with only two wheels if the
reluctant one didn't extend, something he didn't want on a runway that
stuck out into the sea. He made a perfect landing on the 100 gallon drop
tanks, we lifted it with the crane, used the emergency lowering system
and only two wheels extended. We got the other one down and the runway
was cleared in quick time. There was minimal damage to the aircraft, drop
tanks and a couple of aerials on the underside and it was flying again
in a few days after stress checks and minor repairs.
At this time the local authorities were having big problems with drug
and people smugglers who used very fast boats. The authorities had no
boats that were a match for the smuggler's craft so the RAF were asked
if they could help with their RSLs which were capable of well over 20
knots. The RAF said 'yes' and patrols were undertaken with RHK Police
personnel on board. The boat was crewed by RAF personnel including one
armourer who was in charge of the Bren gun on the foredeck. The Bren magazines
were filled with ball and tracer ammunition to fire across the bows of
any boat that was reluctant to stop when instructed. A large number of
boats were stopped over a six-month period and a lot of drugs were found
and illegal immigrants were arrested along with the boat crews. The local
authorities eventually got their own high-speed craft and the RAF involvement
ended.
On the flying side almost everything was normal apart from the fact that
we had a spell of losing brake chutes. For no obvious reason the brake
chute doors would open and the chute would disappear, as the release unit
would operate at the same time. This resulted in the affected aircraft
flying without brake chutes fitted until the electrical fault was rectified.
1962 was drawing to a close and it was time to submit choice of posting
for back in the UK. I remember that one of my choices was St. Mawgan but
not the other two. Eventually my posting came through and I was to go
to St. Mawgan so I was quite pleased. My flight home date was to be 14th
January 1963 on another Britannia of British United Airways to Stansted.
In the meantime the daily routine continued and all was well until the
Friday before Christmas, which was the last working day before the Christmas
shutdown. I was running the line that day and strapped Fl/Lt Crichton
into XE535 for the last flight of the day (year). The gunnery officer
landed in one of the other aircraft and came over to say that there was
thick fog over the sea and to stay local. Fl/Lt Crichton asked me if the
aircraft was fitted with a brake chute to which I replied 'no' and the
aircraft taxied out. After take-off he stayed local and did some aerobatics
over the airfield before going up-country.
On the ground we were all sat in the sunshine
waiting for the aircraft to return and everything not required had been
stowed away for the Christmas break. After a while we heard the aircraft
approaching from behind the ridge at Lion Rock and watched to see it pop
over the ridge for a fast run over the airfield. Only it didn't pop over
the ridge; there was a huge explosion and a pall of black smoke from the
other side of the ridge. I scanned the sky for a parachute hoping the
pilot had ejected but there was none. The RHKAAF helicopter was launched
immediately and flew over the ridge to the crash site and returned to
say that there was no sign of life. Guards were flown up by helicopter
and stayed there overnight until we climbed up there early next morning
to start the investigation. We took up everything we thought we would
require; I remember I had a 4 ½ gall jerry can of water strapped
to my back.
The crash site was about 200 feet below the top of the ridge and was a
hole in the mountainside surrounded by various bits of metal. The Cpl
airframe fitter had previous Hunter experience and his aim was to find
the flapjacks and tail plane actuator. The rest of us just cleaned up
the mess and it was bagged up and sent down to base by helicopter. We
eventually found the flapjacks, which were in the extended position and
the tail plane actuator, which was fully nose up. The airframe guy then
explained to me his theory that, having been doing aerobatics prior to
the accident, if the flaps were inadvertently left down, the faster the
aircraft went it would eventually run out of nose up trim with the inevitable
consequences. This turned out to be the case and was the reason put down
by the board of enquiry as the cause of the accident. The pilot was due
to fly back to the UK with his family at the same time as me. I believe
his father was an Air Commodore. The funeral was held at the military
cemetery on HK Island with full guard of honour and firing party.
We had another pilot, Fl/Lt 'Chunky' I'Anson who was a character. His
bone dome was decorated to resemble a pineapple and I had some 8mm movie
film of him doing a low, slow fly-by on the range in a Venom, with the
canopy open and both arms outstretched in the air stream! I met him again
at Chivenor in 1965 where he was a Qualified Weapons Instructor on Hunters.
I had a holiday in Singapore where I stayed with Pete Shaw (79th Airframes)
and got to ride (Pete's) bikes. They used to have regular sprint meetings
at Seletar and Pete used to compete on his Triumph 5TA. I also met Chris
Conn who was riding the works Honda 250 four and was doing very well on
it. Unfortunately I didn't get to ride that. Anyway, 14th January 1963
arrived and it is time to depart for the UK. Another long haul in a Britannia.
Being only a few weeks after Christmas we weren't aware of the way the
weather had turned in the UK and it was quite a surprise to land on an
ice and snow covered runway at Stansted between banks of snow on the side.
I'm still convinced that if we hadn't had reverse pitch we wouldn't have
stopped! After 2 ½ years in HK the cold was bitter. The drive home
was fairly uneventful and I had six weeks before I had to report to my
new unit at St. Mawgan.

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